Object Oriented Programming (OOP) is supported by many PC programming languages.
How about PLC programming systems? Do you think that object oriented programming is possible for industrial automation systems?
Some automation gurus say that 'object oriented programming is for only programs, an automation system is not a program; may have a program but it is not a program, it is not a desktop application. So automation systems can not be object oriented'
And some gurus say that 'we are already designing in object oriented for many years, before it applied to PC programming'
What do you think?
I will be glad if you write some comments before starting a new post series. Should I define and describe the basics of object oriented design? Or directly run in to a case study of 'object oriented design in an automation system?'
Object Oriented Design in Industrial Automation
INDAFINS - OMRON Fins OCX
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05.12.2009 21:05
INDAFINS sources are uploaded to
http://groups.google.com/group/indanotes/web/OCX.zip
I was planning to publish all source codes by releasing beta version. (INDAFINS is still alpha version).
Unfortunately I don't have too much time to upgrade it. So I have decied to publish source codes of alpha version.
And also I was planning to upgrade INDAFINS as INDAFINS.Net for .Net environment after adding several more functionalities:
- Serial port support
- Read / Write I/O and timers, etc.
Please feel free to modify it,but I have several petitions:
- Please do not remove any links and information about indanotes.blogspot.com and this post.
- Please keep existing comments.
- Please add your name to source code as a comment if you modify it, and send to me to publish new versions here. I promise, I will keep your name also in this historical post.
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26.11.2008 00:35
I have released the documentation. I also realized that bad naming on source codes and fixed them.
You can download them from
http://code.google.com/p/indafins/downloads/list
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19.11.2008 13:32
Google rocks! I decided to host the project at google code instead of sourceforge.
You can download the setup files from
http://code.google.com/p/indafins/downloads/list
Setup file contains the ActiveX and a tester. I am going to publish the source codes soon.
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18.11.2008
An ActiveX controller 'INDAFINS' for OMRON FINS protocol is going to be published.
This posts address will be a permanent link, I am planning to edit this post on each version release.
It is still in alpha version and supporting only read & write data memories and extended memory banks over ethernet UDP.
I am planning to cover at least %90 of FINS protocol. Also I am planning to give FINS over RS 232 in the same ActiveX, so it should be very easy to change an applications communication method just only chancing one single line in a project.
Unfortunately, there is no documentation yet, I am planning to write a draft document as soon as possible.
However, when you are using this ActiveX, please:
- Use it by your own risk, it is not a commertial product. Just a freeware.
- Never place an emergency stop function on your PC applications, PC devices and communications are not stable, you may not stop the system in case of emergency.
- New warnings about INDAFINS can be added to this blog, it would be better to subscribe to RSS feed of this blog to be get informed.
I was planing to publish this ActiveX controller as an open source project in www.sourceforge.net, however I need to study more on CVS to publish on SourceForge.
I am going to find a reliable download host other than rapidshare, I would be glad if someone can offer me a good link.
Operation Times Reporting In an Assembly Line - DB Application
Operation Times Reporting In an Assembly Line - DB Application
In our previous post, we have studied on data collection. In this post, we are going to study on database design.
Let's remember, we were going to deal with more than 30 million records annually in a database, and we were seeking a way to handle it without throttling the database server.
Let's remember what our customer needed:
Operation times distribution as an histogram : Calculating an histogram may be a little bit difficult. We should prefer to display reports which are easily derived with SQL sentences. And displaying 70 stations histogram in a single page may not help to understand bottlenecks.
The box plot graphics seemed the best alternative for histogram. It includes basic information from histogram:
and can present all stations graph in a single page:
Pictures are taken from wiki pages, unfortunately I can't publish samples from customers reports.
Idle time to find out bottle necks: For idle time, less is better. So, what about displaying them with a colourful background? Report data is simple, will just include two rows, 'Station name' for first row and average idle time for the second row. It would be nice to change proportionally the background of the cell for idle time according to idle time. If smaller values are better, we can display minimum idle time in totally green, and maximum idle time in totally red. And the others may be proportionally colourized in a gradient:
- Station number
- Date
- Hour
- Number of products
- Minimum of T1
- Maximum of T1
- Q1 of T1
- Q3 of T1
- Median of T1
- Average of T1
- Standard deviation of T1
- And same calculations same as T1 for T2 and T3 time intervals.
- Half a day for PLC software modification
- Quarter of a day for PC software development
- Quarter of a day for PC summarising task application
- One day for report web pages
Operation Times Reporting In an Assembly Line
In our previous post, I have told about a customers request for reporting operation times of stations in their assembly line.
They were going to use it for assembly line balancing
Many readers may think that 'well, assembly line balancing should be done before establishing the assembly line', you are right.
But our customers assembly line was producing mixed products, I mean there could be several types of product at the same time. In the other hand they had too many types of product, and new types of products were being developed by their R&D department.
If you want to see the performance of stations in your assembly line, what would you like to have in your reports?
- I would like to see the operation times distribution as an histogram.
- I would like to see the idle time to find out bottle necks.
- I would like to see the efficiency of stations.
- I would like to see how mechanical movements limit my productivity
We had a budget limited with only software change, customer did not wanted to add any extra devices or operations on assembly line.
Let's consider our scenario with a single station:
- Station is free.
- New product comes from previous station
- Operator starts working on product.
- Operator pushes the 'operation complete' button to send the product.
- Product waits if the next station is busy.
- Product moves to the next station when the next station is free.
- Station becomes free.
- Product complete button
- Product presence sensor
- A buzzer to warn the operator on exceeding the cycle time
We had to design the system for both convenient for PC and PLC software development.
First we discussed about storing the measured operation times in PLC, then transfer to PC. Not so convenient. There were more than 70 stations, meaning 70 more timers or counters in PLC. For our project it was impossible without PLC upgrade.
And not only operation times of course, we had to think about transfer times and idle times also. It was impossible with customers existing PLC system.
And making necessary software changes in PLC should take at least one week.
So we decided to copy only hardware inputs from PLC to PC. Solving the problem in PC was more convenient.
In PLC, we made two flags:
Product presence flag, which is directly connected to product presence sensor, set to “1” if station is occupied with a product and reset to “0” when station is free.
Let's draw a timing diagram, this is not an handshake, just a timing diagram for two flags:
T1,T2 and T3 shows only one products timing. TA,TB and TC is the next products timing.
Normally T1, T2 and T3 corresponds with TA, TB and TC respectively.
T1 is the time interval that the station is free, however a new product may be on the way.
T2 is exactly the operation time which spend for assembly operations.
T3 is the idle time, where all assembly operations are completed and product is waiting for the next station to become free.
T2 and T3 were the exactly time intervals we would like to see. But, what about transfer time? We also needed to report transfer times.
For an exact transfer time calculation, we have to measure the time between our stations product presence flag and next stations product presence flags rising edge.
However, it is just a little bit difficult because to do this, we also have to consider order of stations to know which station follows which. It was difficult to manage because assembly line was not straight, there were branches and loops.
So we decided to accept that TA as a transfer time.
Why not T1? Also T1 was possible, but we considered that PC is an unstable device, may be frozen or application may hang. So PC software may be restarted anywhere in the cycle and measure time intervals as shorter than it is. We wanted PC to record clear measurements only.
In PLC software, we had represented the flags as bits in a byte, so a single byte stored 4 stations information.
For 70 stations, 18 bytes were enough. PC was going to read 18 bytes from PLC and was going to write 9 bytes for buzzer alarm.
In PC, we have considered all stations as an array, just wrote few lines of code for one station and applied to all stations in a For..Next loop.
Overall code except 'Read all inputs' and 'write all inputs' took less than 100 lines of codes.
Data was collected successfully.
For our next post, I am planning to tell you about the database structure and web page reporting of this project. We had some limitations in DB.
I think may people guessed our problem, there were 70 stations meaning that each product will produce at least (at least because there were some loops in assembly line) 70 records in database.
One shift was producing approximately 600 products.
There were three shifts daily.
Working 5 days in a week.
Working nearly 50 weeks in a year.
So we were expecting:
70 x 600 x 3 x 5 x 50 = 31 500 000
more than 30 million records.
And customer was planning to apply the project to their second assembly line if project not fails.
More than 60 million records. So huge that consumes too much CPU in database server and possibly may slow down other applications.
For the next post, we are going to focus on database design and some statistics.
Customer is always right and sometimes undefined
Simple PC – PLC Communications Part V - Expect The Unexpected
The handshake used for PC – PLC communication works well if everything is perfect. But what happens if something happens that violates the handshake?
In some countries power loss is an ordinary part of life. Generally PC is supplied by UPS, but PLC is not. In a power loss, PLC lefts the communication unexpectedly.
Even if you are using an industrial PC, it is not stable as a PLC. PC or the software running on PC may be frozen. In this case, PC or software may need a restart.
In the other hand, physical conditions may also violate the handshake. Imagine that boxes crashing on station:
It is possible; sensors may be dirty or defected, or any other unexpected reason may cause this.
Most PLC systems use non-volatile memory for holding data permanently. For a PLC system, it is not difficult at all.
If we are programming the PC, it is obvious that we have to store some information in a file or in database to avoid failure after power loss.
- Store all global variables (handshakes last time interval, all counters etc. and the most important; the last data you wrote in to PLC) in to a text file or database as soon as they changed.
- Restore all global variables on start up.
- Do not execute 'Write all outputs' before restoring all global variables.
VB6.0 example:
Public Property Get Data As Integer
Public Property Let Data(ByVal New_Data As Integer)
End Property
'Get' routine is executed whenever you attempt to read property 'Data' as
A = Data
or
And 'Let' routine is executed whenever you attempt to write property 'Data' as:
or
Use 'Property' as a global variable, add a record routine inside 'Let' and never mind again.
For the example above, restoring the 'm_Data' global variable instead of restoring 'Data' is works faster because restoring 'Data' will cause re-recording the 'Data' again and in some cases it may cause a violation error as 'File Already Open'
Rule 3 is also important. Think about the handshake graphics:
C may assign anything in the memory unless variable is initialised.
If it is not possible to control write and reads?
Some SCADA systems also uses 'Read All Inputs' and 'Write All Outputs' routines for PC – PLC communications. However some of them may execute those routines in a separate thread so it may be possible to write a global variables (mostly named as 'Tag' in SCADA systems) value into PLC before initialising or restoring it.
One solution is using a cyclic counter in PLC. PLC has an increasing counter and PC echoes it into another data memory of PLC. If counter value is equal to the echo, PLC increases the counter and waits the same value from PC. If PC can not update in a certain time, PLC understands that PC has failed, and the data from PC is untrusted. This method also can be used to understand if PC is still working.
Fragmanted Information
This may be dangerous if automation system designers don't take sufficient precautions.
Assume that PC is writing a receipt into PLC data memories, and 'receipt ready' flag is at the beginning of the data memory area.
PLC may apply the receipt as soon as it realises 'receipt ready' flag is set, however receipt may not be ready on time. This results of this design may be difficult to debug.
How can we avoid fragmented information?
- We can use checksum at the beginning or at the end of data memory area reserved for PC's write operations. However, there is still a probability that something may leak because there are too many possibilities to produce the same checksum value.
- We can use the counter solution stated above. Reserve two data memories in the data memory area which is reserved for PC's write. Let the PC fill two data memories with the echo from PLC. If both data memories are same and fresh, PLC can trust that information is consistent and trustable.
Our next post will be about customers. 'Customer is always right and mostly undefined'. And we will have another series with a case study. We are going to examine a data collection system to use for assembly line balancing and reporting the bottle necks on an assembly line.
Simple PC – PLC Communications Part IV - Evaluation Code Sample
In this post, I would like to give a simple pseudo code for managing time intervals, how to switch them between. Remember that following code is belong to 'Evaluate' function which is stated in second post and executing in a continious loop:
Global TimeInterval
Function Evaluate()
Select Case TimeInterval
Case "T1"
If PLC_Read.Request = True
TimeInterval = "T2"
End If
Case "T2"
RecordData()
TimeInterval = "T3"
PLC_Write.Response = True
Case "T3"
If PLC_Read.Request = False Then
TimeInterval = "T4"
End If
Case "T4"
TimeInterval = "T1"
PLC_Write.Response = False
End Select
End Function
However, it is just a sample, it is possible to simplify this code into less steps. For example it is possible to insert into database and then switch into last step according to read data from PLC.
For next post, we are going to give some tips about managing steps and increasing immunity against deadlocks may be caused by power loss and operators unwanted, unexpected behaviours.
Simple PC – PLC Communications Part III – Signals with animation
A presentation may explain lots of things than words:
Simple PC – PLC Communications Part II – A Case Study for Product Traceability
In this post, we are going to focus on 'evaluate' part of the algorithm.
It is better to focus on evaluation in a case study, assume that we have three consecutive stations in an assembly line as follows:
If we are studying on a case, we need a scenario. Assume that we have an operator, say 'Mike', on assembly line.
Mike is working on Station Y and he is responsible for checking if boxes are good or not. He has two push buttons, one red and one green. He presses green button for good boxes and presses red for defected. Boxes come from Station X, and left Station Y towards Station Z after Mike's decision.
We also have a barcode reader on Station Y which is directly connected to PLC. A bar code reader connected to a PC requires a little trick that we are going to discuss later.
With Mike and other components, our system should seem as:
Now our goal is collecting information from boxes and matching them with their quality status.
Finally, we want a data table in our PC as follows:
Date Time | Barcode Data | Station | Quality Status |
10.10.2008 16:18:30 | 8463952819456 | Station Y | OK |
10.10.2008 16:19:02 | 8392753021983 | Station Y | NOK |
... | ... | ... | ... |
We can derive several reports with this data, we can use pivot charts to see summary, or we can develop a web page to present our data, it is not in this scope of this post.
When we think over scenario we see that events should happen step by step:
- A new box arrives on Station Y
- Barcode reader scans the barcode (Assuming that it never fails)
- Mike pushes a button
- Data is recorded
- Box leaves Station Y and moves to Station X
- Product presence on station
- Scanned barcode data
- Which button is pushed
- Confirmation of record created successfully.
This handshake protocol is not the one used for PC – PLC communication. For example, it is not FINS protocol of Omron or it is not Modbus protocol.
We are already reading a part of PLC data memory and filling another part continuously with an endless loop, I mean we need a safe method to manage information carried by physical PC – PLC communication.
Following diagram is a sample protocol that can be used for our case:
Our next post we will continue on the same case study.
We are going to discuss:
- What happens in T1, T2, T3 and T4 intervals ?
- How can we organise internal structure of evaluation algorithm ?
- Few tips about design